Crude Rationalization (2018)

Sep 2018 – Dec 2018

Alarm rationalization for CDU unit at 380,000 BPD refinery. Completed on schedule and under budget. Net alarm reduction 38%. Averaged 52 tags /d (7 h).
  • Facilitated alarm rationalization efforts for Crude Distillation / Gas Compression (CDU/GCP) unit at the company’s flagship 380,000 bpd refinery.
  • Rationalized DCS and SIS systems on this unit to corporate standards.
  • Coached project team on best-practices for alarm rationalization.